Operational guide to stabilize, standardize and increase power plant efficiency
Complex engineering systems, such as power plants, deliver their best performance when operating along a designed range of some priority parameters. However, plant field operation may deviate from design conditions, and new references must be identified. Actions towards high-quality operation can be...
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Published in | Applied energy Vol. 315; p. 118973 |
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Main Authors | , , , , , , , , , |
Format | Journal Article |
Language | English |
Published |
Elsevier Ltd
01.06.2022
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Subjects | |
Online Access | Get full text |
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Summary: | Complex engineering systems, such as power plants, deliver their best performance when operating along a designed range of some priority parameters. However, plant field operation may deviate from design conditions, and new references must be identified. Actions towards high-quality operation can be supported by fine modeling, which helps building decision support tools. The present work proposes a standardization strategy for the operation of an actual coal-fired power plant based on a Design of Experiment approach, partially tested onsite and finally accomplished with surrogate models built upon a 2 year long database. Artificial Neural Networks (ANNs) and Mass and Energy balances (M&Es) are used to represent the plant’s steam generator and its mills subset, which is the core of an operational guide to increase system efficiency under actual operation. Primary and secondary air flows, pulverized coal outlet temperature, speed of the dynamic classifier, primary air flow, excess O2, primary and secondary air pressures are the seven controllable factors selected as the most relevant ones among an extensive set of parameters, able to perform effective maneuvers. The application of the operational guide indicates combinations of ranges of the seven controllable parameters that allow for achieving steam generator efficiency within the 84.0% to 88.92% range. The proposed methodology aims as well to improve safe and stable conditions to a system that undergoes operation different than the one prescribed by the original design. The study case results show an opportunity to raise efficiency by up to 2.28% during operation, which represents a reduction in coal consumption by 3.1 t/h and above 6% on CO2 emissions.
•Real plant data, operational information and real experiments on site from the PECEM power plant.•System performance process standardization employing decision support tools.•A high-quality operation by the fine modeling of plants systems.•Surrogate models applied on coal-fired power plants literature reviewed.•Logbook to perform a Design of Experiments approach in a power plant in operation. |
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ISSN: | 0306-2619 1872-9118 |
DOI: | 10.1016/j.apenergy.2022.118973 |